![]() |
#1 |
Furball
Join Date: Oct 2020
Location: North Carolina
Posts: 112
Vehicle: 1994 XE King Cab
Thanks: 3
Thanked 21 Times in 18 Posts
|
![]()
I’m having a bastard of a time tracking down this intermittent stumble in my V6 so I need to pick some brains.
I have replaced many vacuum hoses and couldn’t find a leak using smoke. The O2 sensor has been replaced. I cleaned the MAF while the manifold was off the truck. All the injectors are brand new and have brand new o rings and seals. The distributor is new, the spark plugs are new, and the plug wires are new. Any thoughts?
__________________
Last edited by KivPanther; 02-19-2021 at 09:47 PM. |
![]() |
![]() |
![]() |
#2 |
4/86 SE-V6 2 tone 4x4 HB
Join Date: Apr 2013
Location: Oregon
Posts: 7,374
Vehicle: 1986.5 SE-V6 4WD D21, 2003 Audi A4 Avant 3.0 Quattro
Thanks: 891
Thanked 903 Times in 822 Posts
|
![]()
Any codes? How old are your plugs and wires?
__________________
1986.5 SE-V6 4X4 D21 Hardbody
Pacesetter Long Tube Headers Morimoto Mini D2S HID Projectors and Hella 500s VG33i ![]() |
![]() |
![]() |
![]() |
#3 |
Furball
Join Date: Oct 2020
Location: North Carolina
Posts: 112
Vehicle: 1994 XE King Cab
Thanks: 3
Thanked 21 Times in 18 Posts
|
![]()
No codes. Plugs and wires are brand new. NGK iridium plugs (real ones) and NGK blue wires.
__________________
|
![]() |
![]() |
![]() |
#4 |
Join Date: Dec 2020
Location: Lakeland, FL
Posts: 30
Vehicle: 1995 Hardbody XE V6
Thanks: 4
Thanked 1 Time in 1 Post
|
![]()
It happens while in cruise control? Maybe the cruise mechanism is going out. Try smoking the cruise control mechanism. It also runs off vacuum
|
![]() |
![]() |
![]() |
#5 |
Join Date: Dec 2020
Location: Lakeland, FL
Posts: 30
Vehicle: 1995 Hardbody XE V6
Thanks: 4
Thanked 1 Time in 1 Post
|
![]()
Also, I'd check your injectors. I have an f150 that I chased a miss I thought was a vacuum leak. Turned out to be a bad injector
|
![]() |
![]() |
![]() |
#6 |
Furball
Join Date: Oct 2020
Location: North Carolina
Posts: 112
Vehicle: 1994 XE King Cab
Thanks: 3
Thanked 21 Times in 18 Posts
|
![]()
Sorry, I should clarify: It doesn't happen ONLY while in cruise control, it happens ALSO while in cruise control. I actually just replaced the ASCD vacuum hose since it had rotted, but it has its own vacuum pump separate from the engine control system. The fuel injectors are, as mentioned above, all brand new, tested working, and getting pulse.
__________________
|
![]() |
![]() |
![]() |
#7 |
Ol'school Geek
Join Date: Mar 2020
Location: Washington State
Posts: 481
Vehicle: 89' D21 KC SE V6 5spd 2WD - 87' D21 KC SE V6 5spd 2WD
Thanks: 499
Thanked 123 Times in 106 Posts
|
![]()
If you replaced the vac line to the cruise, what condition was it in? Could be some smaller particulates got pulled in? ...from the inside of the old rotted hose? (thinking outloud)
|
![]() |
![]() |
![]() |
#8 |
Furball
Join Date: Oct 2020
Location: North Carolina
Posts: 112
Vehicle: 1994 XE King Cab
Thanks: 3
Thanked 21 Times in 18 Posts
|
![]()
The ASCD itself is old it in good shape. The only thing bad was the vacuum hose. Still though, since it does it regardless of whether I’m in cruise control or not I doubt it’s related.
__________________
|
![]() |
![]() |
Thanked by: | 89'HBV6 (02-19-2021) |
![]() |
#9 |
Join Date: Jul 2015
Location: N.E. Kansas
Posts: 730
Vehicle: 1990 Nissan Hardbody
Thanks: 0
Thanked 99 Times in 87 Posts
|
![]()
So no change between before/after the new injectors?
It seems that the problem would be more evident under hard acceleration if fuel-flow was the cause, but did you change the fuel filter too? If it is repeatable, try cracking the gas cap open and trying it again. Might generate an error code, but is the miss gone?
__________________
Original owner
1990 Nissan Hardbody, Aztec Red Standard cab, 4x4, KA24E, 5-speed Intentionally near-stock ![]() Mods: Second OEM horn, stereo/speakers/sub, mud and snow tires, HD trailer hitch (cat 3+), liquid bed liner, G1W dashcam Definitely not for sale! ![]() |
![]() |
![]() |
![]() |
#10 |
Furball
Join Date: Oct 2020
Location: North Carolina
Posts: 112
Vehicle: 1994 XE King Cab
Thanks: 3
Thanked 21 Times in 18 Posts
|
![]()
Correct; there was no change after the injectors were replaced. I did replace the fuel
filter at the same time. I had bought a new TPS but hadn’t gotten around to installing it yet since I wasn’t sure it would need it. I also haven’t been able to get the idle to drop all the way to 750 after warming up even after adjustment. I might just go ahead and swap them just in case. I’ll give the gas cap thing a go on my way home from shift tonight and see what happens.
__________________
|
![]() |
![]() |
![]() |
Thread Tools | |
Display Modes | |
|
|